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Purpose

This paper aims to analyze a failure case of a P110 tube in a CO2 flooding well.

Design/methodology/approach

The chemical composition, microstructure and mechanical properties of the failed P110 tubing steel were tested, and met the API Spec 5CT standard. The fractures were investigated by scanning electron microscopy and energy dispersive spectroscopy.

Findings

Fracture was induced by stress corrosion cracking (SCC) and that the stress concentration caused by the mechanical damage played an important role in the failure. The failure case is a SCC failure affected by mechanical damage and galvanic corrosion.

Originality/value

The effect of the infiltration of groundwater was studied in the failure case. The stress concentration caused by the mechanical damage played an important role in the failure.

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