– The purpose of this article is to illustrate how the Six Sigma methodology was applied to a small-scale foundry industry to reduce the rejections and rework in one of its processes.
– The research reported in this paper is based on a case study carried out in an industry using the Six Sigma Define-Measure-Analyze-Improve-Control (DMAIC) approach and its application in improving the leaf spring manufacturing process of a foundry shop.
– The root causes for the problem of rejection and rework were identified through data-based analysis at different stages in the project. The process parameters were optimized and measures for sustainability of the results were incorporated in the process. As a result of this study, the overall rejection was reduced from 48.33 to 0.79 per cent, which was a remarkable achievement for this small-scale industry. This was leading to improvement in on-time delivery to the customer. The finance department of the company estimated the annualized savings due to the reduction in rejection and was to the tune of USD8,000 per year.
– The paper is based on a single case study executed in a company, and hence, there is limitation in generalizing the specific results from the study. However, the approach adopted and the learning from this study can be generalized.
– This article illustrates the step-by-step application of Six Sigma DMAIC methodology in a small-scale foundry industry to solve an age-old problem in the organization. Thus, this article will be helpful for those professionals who are interested in implementing Six Sigma to such industries.
