Viable remediation of the large lateral deformation of high-speed railway (HSR) subgrades, especially in soft soil areas, is still absent. An integrated rectification scheme of high-pressure jet-grouting (HPJG) combined with stress-release techniques was conducted to rectify the large lateral deformation of an operational HSR subgrade in the soft soil area of China, but without any refined design and mechanical analysis before rectification due to the emergency. The objective of the study is to post-evaluate the rectification effects utilising field monitoring data and numerical calculations. The monitoring data showed that the maximum lateral deviation of the subgrade was 69.1 mm, which almost met the expected correction requirements. However, the influence of the excess pore water pressure (EPWP) dissipation on the correction deviation was not considered in the scheme. Therefore, a numerical model was established to further investigate this effect and corresponding mitigation methods. The calculated results revealed that EPWP in the foundation dissipated mostly within 6 months after rectification, and the deformation loss accounted for 30.7% of the total deviation. Prolonging the interval of two-row pile construction can be a plausible approach to mitigate the deviation loss. The findings provide a feasible method for correcting large lateral deformation of HSR subgrades.
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April 2025
Research Article|
February 29 2024
Correction effect of jet-grouting on high-speed railway subgrade lateral deformation Available to Purchase
Yingqi Bai, BEng;
Yingqi Bai, BEng
PhD candidate, Shanghai Key Laboratory of Rail Infrastructure Durability and System Safety, Key Laboratory of Road and Traffic Engineering of the Ministry of Education, Tongji University, Shanghai, PR China
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Junhua Xiao, PhD;
Junhua Xiao, PhD
Professor, Shanghai Key Laboratory of Rail Infrastructure Durability and System Safety, Key Laboratory of Road and Traffic Engineering of the Ministry of Education, Tongji University, Shanghai, PR China (corresponding author: jhxiao@tongji.edu.cn)
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Lihua Xue, BEng;
Lihua Xue, BEng
PhD candidate, Shanghai Key Laboratory of Rail Infrastructure Durability and System Safety, Key Laboratory of Road and Traffic Engineering of the Ministry of Education, Tongji University, Shanghai, PR China
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Zhiyong Liu, PhD;
Zhiyong Liu, PhD
Professor, Shanghai Key Laboratory of Rail Infrastructure Durability and System Safety, Key Laboratory of Road and Traffic Engineering of the Ministry of Education, Tongji University, Shanghai, PR China
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Binglong Wang, PhD
Binglong Wang, PhD
Professor, Shanghai Key Laboratory of Rail Infrastructure Durability and System Safety, Key Laboratory of Road and Traffic Engineering of the Ministry of Education, Tongji University, Shanghai, PR China
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Publisher: Emerald Publishing
Received:
September 25 2023
Accepted:
February 22 2024
Online ISSN: 1751-8563
Print ISSN: 1353-2618
Emerald Publishing Limited: All rights reserved
2025
Proceedings of the Institution of Civil Engineers - Geotechnical Engineering (2025) 178 (2): 133–145.
Article history
Received:
September 25 2023
Accepted:
February 22 2024
Citation
Bai Y, Xiao J, Xue L, Liu Z, Wang B (2025), "Correction effect of jet-grouting on high-speed railway subgrade lateral deformation". Proceedings of the Institution of Civil Engineers - Geotechnical Engineering, Vol. 178 No. 2 pp. 133–145, doi: https://doi.org/10.1680/jgeen.23.00169
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